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                                      118 
                                      passengers were on board British Midland 
                                      flight 92 when it departed London's 
                                      Heathrow airport bound for Belfast on the 
                                      evening on January 8, 1989. Captain Hunt 
                                      and his First Officer, along with six 
                                      other cabin crew members brought the total 
                                      on board the 737 to 126. Flight 92 
                                      departed just before 8pm and was promptly 
                                      cleared to FL350. Just after 8pm, while 
                                      passing through FL280, there was a loud 
                                      noise, the aircraft began to vibrate, and 
                                      light smoke entered the cabin area through 
                                      the air conditioning system. Passengers in 
                                      the rear of the aircraft reported seeing 
                                      flames coming from the port side engine. 
                                      On the flight deck, though the crew could 
                                      feel the vibrations and smell smoke, there 
                                      were no aural or visual warnings. 
                                      
                                       
                                      
                                      Wreckage of 92 
 
                                      Captain 
                                      Hunt disengaged the autopilot and took 
                                      control of the aircraft. There were no 
                                      anomalies in the engine indications, but 
                                      believing that the air conditioning 
                                      received bleed air from the right engine, 
                                      Hunt believed the difficulty was coming 
                                      from there. Hunt throttled back the right 
                                      engine and both the vibrations and the 
                                      smoke seemed to decrease. The First 
                                      Officer called London ATC to report the 
                                      emergency. Hunt initially ordered the 
                                      engine be shut down, but before it could 
                                      be done, Hunt decided that the engine 
                                      seemed to be running satisfactorily and to 
                                      keep it running. At this point, they were 
                                      only minutes away from Castle Donington 
                                      airport, which was British Midland's 
                                      maintenance facility, so Hunt decided to 
                                      divert there. Having made the decision to 
                                      divert and being cleared for a descent, 
                                      Hunt then advised the First Officer to 
                                      proceed with the shutdown of the starboard 
                                      engine.  The Captain then made 
                                      an announcement on the PA that he had shut 
                                      down the right engine and that they would 
                                      be landing shortly. Apparently none of the 
                                      passengers who saw flames from the left 
                                      engine either heard the captain or felt 
                                      that they were in position to say anything 
                                      about it. The aircraft descended normally 
                                      except for continued vibrations and the 
                                      crew intercepted the localizer for runway 
                                      27 at Castle Donington at 2,000ft and 
                                      began it's descent down the glideslope 
                                      just four miles from the runway.  At 900ft and 2.5 miles 
                                      from touchdown, the left engine completely 
                                      lost power. The captain called for a 
                                      relight on the right engine and several 
                                      seconds later, the engine fire lights came 
                                      on from the left engine. The Captain just 
                                      had time to call for emergency brace over 
                                      the PA before the aircraft impacted the 
                                      ground at 110kts, just three-quarters of a 
                                      mile from the runway. The aircraft bounced 
                                      off the embankment, went across a motorway 
                                      and into the other side of the embankment, 
                                      fracturing the fuselage and flipping the 
                                      tail section over. Thirty nine passengers 
                                      were killed in the impact and eight others 
                                      died later. It's highly unlikely that both engines 
                                      would fail concurrently, so investigators 
                                      were very anxious to examine the wreckage 
                                      for clues as to what caused a total loss 
                                      of power on flight 92.
 
                                      Both 
                                      engines suffered extensive impact damage 
                                      and a great deal of debris was lodged 
                                      inside the forward sections. Interior 
                                      inspection of the engines, however, 
                                      revealed major differences between the 
                                      condition of the two. The right engine 
                                      showed only ground impact damage and it 
                                      was clear that the engine was not running 
                                      at the time of the crash.  
                                      
                                          Wreckage of 92 
 The left engine, 
                                      however, showed severe fire damage and 
                                      several blade fragments were missing, some 
                                      recovered along the flight path as far 
                                      away as a mile and a half from the crash 
                                      site. It was clear that the left engine 
                                      had been the one which had suffered 
                                      mechanical difficulty during flight. So 
                                      what then would cause the crew to shut 
                                      down the good engine?Recovery of the CVR and FDR showed that, 
                                      during the initial period of vibration and 
                                      smoke, there were large variations in N1 
                                      and EGT indications as well as low fuel 
                                      flow. When asked which engine was causing 
                                      trouble, the First Officer replied "It's 
                                      the le...it's the right one." The FDR 
                                      shows at this time that all right engine 
                                      indications were normal. The FDR also 
                                      showed that when the right throttle was 
                                      closed, the left engine indications 
                                      returned to near normal with the exception 
                                      of the fuel flow, which was still erratic. 
                                      Hunt attempted to discuss with the First 
                                      Officer what indications had been 
                                      received, but radio calls prevented them 
                                      from further examining their situation.
 
                                      Further 
                                      study of the left engine showed that the 
                                      fire had occurred after the crash. The 
                                      initial cause of engine damage was the 
                                      fatigue failure of one of the fan blades 
                                      and further overload failure of the rest 
                                      of the blades. It was clear then that the 
                                      right engine was functional throughout the 
                                      flight and the crew had somehow 
                                      misidentified it. 
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