September 20, 1989 brought cold and wet weather 
            to New York's LaGuardia Airport. USAir's flight 5050 was preparing 
            to depart for Charlotte, North Carolina with 57 passengers on board 
            along with four flight attendants. On board the flight deck of the 
            737 were Captain Micheal Martin and First Officer Constantine 
            Kleissas. 
        
       
       Wreckage of 5050
            
            The 
            crew had a long layover in New York and was forced to wait for 
            nearly and hour and a half due to weather. Finally at about 11:30pm 
            the aircraft was cleared for takeoff with Kleissas at the controls. 
            As the aircraft picked up speed on the takeoff roll, it began to 
            drift to the left. The crew decided to abort the takeoff, but the 
            aircraft was still rolling when it reached the end of the runway, 
            plunging into Flushing Bay. The fuselage broke up and came to rest 
            on the approach lights. Two people were killed.
            
            The crew reported that the aircraft began to drift during the 
            takeoff roll which Kleissas attempted to counteract with rudder 
            inputs. The aircraft continued to drift and Martin then attempted to 
            assist by using the nosewheel steering tiller. The crew then 
            reported hearing a bang followed by continued rumbling. At this 
            point, the abort decision was made. The aircraft had accelerated to 
            nearly 140kts however, and due to the wet conditions of the runway, 
            could not be stopped in time. 
            Investigators believed the rumbling sound to have 
            been the nose wheel turning and then sliding down the runway. 
            Recovery of the FDR showed that the rudder trim had been left in the 
            full left deflection position throughout the takeoff. in fact, it 
            had been in that position since the aircraft was started at the 
            gate. This would normally be an item on the pre-takeoff checklist 
            and recovery of the CVR indicated that the crew had checked the 
            rudder trim during the checklist. 
            It was not determined whether a mechanical 
            malfunction caused the rudder to be out of position or if the crew 
            had simply missed catching it. Investigators concluded that Martin's 
            hesitation on making the decision to abort was the cause of the 
            accident. Martin had only just been upgraded to Captain and 505 was 
            Kleissas' first non-supervised flight.